The little guy is rapidly approaching SIX pounds now, and is drinking around 90% of his bottle.
Bigger and bigger, stronger and stronger as they days go by. Medical advances for premies are astounding. It wasn't that long ago his chances of survival at 10 weeks early would have been pretty slim.
We'll be seeing him in about a month, and I get to hold him.
Wonder if he'll grab at my beard......
Admiral Yamamoto infamously said "You cannot invade the mainland United States. There would be a man with a rifle behind every blade of grass."
And so it should be, a nation of riflemen....
Tuesday, April 25, 2017
Saturday, April 22, 2017
Happy Earth Day!
The USAF wishes all our terrorist friends a very Happy Earth Day!
Your gifts should be arriving shortly.....
Your gifts should be arriving shortly.....
Thursday, April 20, 2017
"The X-Files" Is Coming Back Again....
According to this article over at CNET, Fox has signed up for another 10 episodes.
And that reminds me....I still haven't watched the six episodes I recorded the last time it "came back"....
Something to do this weekend while the wife is visiting her friend.
And that reminds me....I still haven't watched the six episodes I recorded the last time it "came back"....
Something to do this weekend while the wife is visiting her friend.
Wednesday, April 19, 2017
Busy Day
Spent the day on the Iowa doing radio stuff, and in meetings.
Museum Ship's Weekend is coming up, so I have a few things to tinker together for the Grey Radio Gang, namely another little adapter box so they can interface a "Red Phone" with a laptop to route some audio to the Combat Engagement Center.
But before that, we have the Armed Forces Crossband Test coming up. This is a test whereby we'll be allowed to transmit on approved DoD frequencies, and listen on the Amateur Radio frequencies.
Sometime back, one of our members was able to contact the guys that do USN ship callsign assignments. He also contacted the USCG Heron, which was using the callsign NEPM at the time.
The importance of the USN callsign NEPM is that it's the callsign originally issued to the USS Iowa when she was commissioned.
The Captain of the Heron was more than willing to release the callsign, and in exchange we helped him get NHRN, an exchange that made both sides happy.
We now have authorization to use NEPM, "In Perpetuity", from the DoD, and we'll take the Iowa on-the-air, using the 1980's ship's legacy radio gear, on May 11th this year.
This will be the first time the Iowa has been on-the-air with NEPM in 27 years.
Museum Ship's Weekend is coming up, so I have a few things to tinker together for the Grey Radio Gang, namely another little adapter box so they can interface a "Red Phone" with a laptop to route some audio to the Combat Engagement Center.
But before that, we have the Armed Forces Crossband Test coming up. This is a test whereby we'll be allowed to transmit on approved DoD frequencies, and listen on the Amateur Radio frequencies.
Sometime back, one of our members was able to contact the guys that do USN ship callsign assignments. He also contacted the USCG Heron, which was using the callsign NEPM at the time.
The importance of the USN callsign NEPM is that it's the callsign originally issued to the USS Iowa when she was commissioned.
The Captain of the Heron was more than willing to release the callsign, and in exchange we helped him get NHRN, an exchange that made both sides happy.
We now have authorization to use NEPM, "In Perpetuity", from the DoD, and we'll take the Iowa on-the-air, using the 1980's ship's legacy radio gear, on May 11th this year.
This will be the first time the Iowa has been on-the-air with NEPM in 27 years.
Sunday, April 16, 2017
Happy Easter!
To all my friends....
Cooking a big dinner today, and the wife's oldest son, his GF, and his daughter will be joining us.
Cooking a big dinner today, and the wife's oldest son, his GF, and his daughter will be joining us.
The Story of an Old Firebird, Part 5....
This section will cover the body/chassis, and the “weight loss program” I put the car on.
The car as delivered handled extremely well. With the 1.25” front sway bar and the .875” rear sway bar, high-rate springs, and Pliacell shock absorbers, it cornered flat. I added Koni adjustable shock absorbers, and set them about half way between very little damping, and break your teeth. The special variable-ration power steering that came with the Y99 handling package, and the small diameter fat-rimmed “Formula” steering wheel made the car steer like a Go Kart. During the course of construction, I cut a full coil from the front springs, and made some lowering blocks for the rear leaf springs. Cutting coils off a spring not only lowers the car, but also raises the effective spring rate. The “best” way to do it is to get shorter springs made, or find some others in the parts book that do what you want, but cutting a coil off is a pretty cheap, effective way to drop the car.
The rear lowering blocks were 3/4” think aluminum blocks I had made at Tubby Gallup’s (I’m pretty sure that’s his name...it’s been almost 40 years!) place, and he also fabbed some longer U-Bolts for me. Adding lowering blocks pushes the rear axle up into the chassis, dropping the body down lower over the axle.
I also ordered some solid body mounts from Herb Adams’ “Very Special Equipment” catalog, along with some front subframe reinforcing struts. The solid body mounts eliminated any deflection caused by the big rubber “biscuit” type body mounts, and moved the front subframe about 3/4” closer to the unibody, effectively “channeling” the body down over the frame. The front struts he sold attached to the pinch-weld area of the firewall in two places, and then ran down to the forward stud for the upper control arm. You loosened the big nut used for front end alignment, remover some alignment shims, dropped the tab on the end of the strut in place, and tightened the nut back up. A trip to the alignment shop was required, as removing the wrong amount of shims had adverse effects on your front camber and caster!
With the cut front springs and the aluminum subframe mounts, the front dropped about 1-1/2 inches. Along with the 3/4” drop in the rear, the car had a pretty mean appearance. Today we’d say it had “Stance”, but back then we just said it was lowered, or had “a mean rake”.
The front and rear sway bar mounts were also changed from rubber to aluminum where the bars mounted to the frame, and the end links were replaced with new ones fabricated using spherical rod ends, or “Heim Joints”. This completely eliminated any deflection in the bar mounting, and made the bars act instantly, rather than having to take up any “squish” or slack in a rubber mount. I didn’t go “Full Race” on the suspension by replacing the front control arm bushings with solid ones, as I’d had before-and-after rides in cars that had that done to them, and it 100% completely ruined the car for street use. You can get away with that on a nice, smooth race track, but solid suspension bushings on the street are completely unlivable. These days we have polyurethane suspension bushings (I have them in my Supra), and while they’re stiffer than OEM bushings, they’re nothing like metal ones.
The only other change I did was to replace the OEM idler arm in the steering linkage with a heavy duty one made by Moog. The arm itself was much thicker, and the bracket where it attached to the frame was twice as thick as the OEM idler arm. It also had grease fittings on both pivots.
So that was it for the chassis. Pretty stock, really, with just a few carefully chosen aftermarket parts.
I already knew that the engine was going to be pretty stout, and without spending a significantly greater amount of money, it was going to make about as much power as I could reasonably expect, which led me to ponder what else could I do to make it faster?
A famous race car designer once said: “More power makes you faster on the straights; Less weight makes you faster everywhere”.
OK, I’ll make it lighter! But how?
There’s an old saying in the aircraft industry: “The best way to remove one hundred pounds is to find 1600 places and remove one ounce”.
I took both sayings to heart, and started looking for “1600 places to remove one ounce”!
Since this was going to be a one or two passenger vehicle, and was not going to be a daily driver, the back seat, seat belts, and mounting hardware could be pulled out. This saved 30 pounds, and got me thinking about how to get more weight out of the car.
Since I was going to relocate the battery out of the engine compartment for better weight distribution, I had to pull the carpet out to run the new cable. I had to pull the front seats (35 pounds each!) out of the car to get the carpet out, and I noticed all these asphalt-and-paper sound deadening pads absolutely everywhere. They were under the carpet, under the seats, under the dash, stuck to the firewall...just all over the place. After I pulled them all out and dumped them on the scale, I realized I’d just pulled another 25 pounds out of the car! This got me really going.
The F60-15 spare tire on the 15x7 steel rim, along with the jack, jack base, handle, and J-bolt and wingnut, weighed in at a staggering 75 pounds.
The new, lighter Corbeau GT bucket seats I was going to use weighed 40 pounds less then the seats the car came with.
All the reinforcing bars and struts, and the mounts and their hardware, for the “5MPH” front bumper weighed 50 pounds. I wouldn’t need them as I was already in the process of pulling a mold off the front Endura bumper so I could replicate it in fiberglass, so out they went.
The fiberglass front bumper replacement I eventually wound up with removed another 100 pounds from the car.
Removing the stock exhaust system, muffler, pipes, hangers, and hardware saved another 70 pounds.
The aluminum intake manifold was 15 pounds lighter than stock, and the aluminum brackets and smaller hardware I used for the rear bumper saved 5 pounds.
There were numerous other brackets that I fabricated out of aluminum, painted them black, and when they were on the car, nobody knew. These saved another 10 pounds.
Any place there was a non-critical fastener, bracket, strut, or other fiddly bit, I either eliminated it, made it out of aluminum, drilled holes in it, and/or used a smaller size bolt to hold it on. Nobody ever saw most of these “little things”, but I wound up with a car that was a real sleeper.
The lighter flywheel and clutch assembly was a wash because I replaced the aluminum bellhousing with a Lakewood scatter shield and block plate. I’d seen cars where the clutch let go, and it did quite a bit of damage, and I wasn’t going to let that happen. Plus, the weight was within the wheel base, and mounted down low, so I didn’t worry about it.
And what’s almost as important as removing the weight was where I removed it from. Most of the weight came off the nose of the car, as in the case of the battery. The 40 pound battery, which was located in front of the engine, and right at the top of the radiator, was moved to the floor of the car behind the passenger seat where the rear seat had been. This got that amount of weight within the wheelbase, and about 24” lower than it had been. A small thing, but “small things” like that can improve the handling of the car, making it easier to turn, and lowering the center of gravity, resulting in flatter cornering.
The total weight savings amounted to over 400 pounds, or more than 10% of the weight of the car.
I didn’t go full-on, bat guano crazy ripping things out, but I did get a significant amount of weight out of the car.
I still had windshield washers and wipers, a fully functional heater, carpeting, my center console, an AM/FM stereo radio, and the side impact beams in the doors of the car, one of the reasons the doors on a second generation F-Body weighed so much.
But it was quite a bit lighter than stock 73 Firebird, and it was worth it.
The car as delivered handled extremely well. With the 1.25” front sway bar and the .875” rear sway bar, high-rate springs, and Pliacell shock absorbers, it cornered flat. I added Koni adjustable shock absorbers, and set them about half way between very little damping, and break your teeth. The special variable-ration power steering that came with the Y99 handling package, and the small diameter fat-rimmed “Formula” steering wheel made the car steer like a Go Kart. During the course of construction, I cut a full coil from the front springs, and made some lowering blocks for the rear leaf springs. Cutting coils off a spring not only lowers the car, but also raises the effective spring rate. The “best” way to do it is to get shorter springs made, or find some others in the parts book that do what you want, but cutting a coil off is a pretty cheap, effective way to drop the car.
The rear lowering blocks were 3/4” think aluminum blocks I had made at Tubby Gallup’s (I’m pretty sure that’s his name...it’s been almost 40 years!) place, and he also fabbed some longer U-Bolts for me. Adding lowering blocks pushes the rear axle up into the chassis, dropping the body down lower over the axle.
I also ordered some solid body mounts from Herb Adams’ “Very Special Equipment” catalog, along with some front subframe reinforcing struts. The solid body mounts eliminated any deflection caused by the big rubber “biscuit” type body mounts, and moved the front subframe about 3/4” closer to the unibody, effectively “channeling” the body down over the frame. The front struts he sold attached to the pinch-weld area of the firewall in two places, and then ran down to the forward stud for the upper control arm. You loosened the big nut used for front end alignment, remover some alignment shims, dropped the tab on the end of the strut in place, and tightened the nut back up. A trip to the alignment shop was required, as removing the wrong amount of shims had adverse effects on your front camber and caster!
With the cut front springs and the aluminum subframe mounts, the front dropped about 1-1/2 inches. Along with the 3/4” drop in the rear, the car had a pretty mean appearance. Today we’d say it had “Stance”, but back then we just said it was lowered, or had “a mean rake”.
The front and rear sway bar mounts were also changed from rubber to aluminum where the bars mounted to the frame, and the end links were replaced with new ones fabricated using spherical rod ends, or “Heim Joints”. This completely eliminated any deflection in the bar mounting, and made the bars act instantly, rather than having to take up any “squish” or slack in a rubber mount. I didn’t go “Full Race” on the suspension by replacing the front control arm bushings with solid ones, as I’d had before-and-after rides in cars that had that done to them, and it 100% completely ruined the car for street use. You can get away with that on a nice, smooth race track, but solid suspension bushings on the street are completely unlivable. These days we have polyurethane suspension bushings (I have them in my Supra), and while they’re stiffer than OEM bushings, they’re nothing like metal ones.
The only other change I did was to replace the OEM idler arm in the steering linkage with a heavy duty one made by Moog. The arm itself was much thicker, and the bracket where it attached to the frame was twice as thick as the OEM idler arm. It also had grease fittings on both pivots.
So that was it for the chassis. Pretty stock, really, with just a few carefully chosen aftermarket parts.
I already knew that the engine was going to be pretty stout, and without spending a significantly greater amount of money, it was going to make about as much power as I could reasonably expect, which led me to ponder what else could I do to make it faster?
A famous race car designer once said: “More power makes you faster on the straights; Less weight makes you faster everywhere”.
OK, I’ll make it lighter! But how?
There’s an old saying in the aircraft industry: “The best way to remove one hundred pounds is to find 1600 places and remove one ounce”.
I took both sayings to heart, and started looking for “1600 places to remove one ounce”!
Since this was going to be a one or two passenger vehicle, and was not going to be a daily driver, the back seat, seat belts, and mounting hardware could be pulled out. This saved 30 pounds, and got me thinking about how to get more weight out of the car.
Since I was going to relocate the battery out of the engine compartment for better weight distribution, I had to pull the carpet out to run the new cable. I had to pull the front seats (35 pounds each!) out of the car to get the carpet out, and I noticed all these asphalt-and-paper sound deadening pads absolutely everywhere. They were under the carpet, under the seats, under the dash, stuck to the firewall...just all over the place. After I pulled them all out and dumped them on the scale, I realized I’d just pulled another 25 pounds out of the car! This got me really going.
The F60-15 spare tire on the 15x7 steel rim, along with the jack, jack base, handle, and J-bolt and wingnut, weighed in at a staggering 75 pounds.
The new, lighter Corbeau GT bucket seats I was going to use weighed 40 pounds less then the seats the car came with.
All the reinforcing bars and struts, and the mounts and their hardware, for the “5MPH” front bumper weighed 50 pounds. I wouldn’t need them as I was already in the process of pulling a mold off the front Endura bumper so I could replicate it in fiberglass, so out they went.
The fiberglass front bumper replacement I eventually wound up with removed another 100 pounds from the car.
Removing the stock exhaust system, muffler, pipes, hangers, and hardware saved another 70 pounds.
The aluminum intake manifold was 15 pounds lighter than stock, and the aluminum brackets and smaller hardware I used for the rear bumper saved 5 pounds.
There were numerous other brackets that I fabricated out of aluminum, painted them black, and when they were on the car, nobody knew. These saved another 10 pounds.
Any place there was a non-critical fastener, bracket, strut, or other fiddly bit, I either eliminated it, made it out of aluminum, drilled holes in it, and/or used a smaller size bolt to hold it on. Nobody ever saw most of these “little things”, but I wound up with a car that was a real sleeper.
The lighter flywheel and clutch assembly was a wash because I replaced the aluminum bellhousing with a Lakewood scatter shield and block plate. I’d seen cars where the clutch let go, and it did quite a bit of damage, and I wasn’t going to let that happen. Plus, the weight was within the wheel base, and mounted down low, so I didn’t worry about it.
And what’s almost as important as removing the weight was where I removed it from. Most of the weight came off the nose of the car, as in the case of the battery. The 40 pound battery, which was located in front of the engine, and right at the top of the radiator, was moved to the floor of the car behind the passenger seat where the rear seat had been. This got that amount of weight within the wheelbase, and about 24” lower than it had been. A small thing, but “small things” like that can improve the handling of the car, making it easier to turn, and lowering the center of gravity, resulting in flatter cornering.
The total weight savings amounted to over 400 pounds, or more than 10% of the weight of the car.
I didn’t go full-on, bat guano crazy ripping things out, but I did get a significant amount of weight out of the car.
I still had windshield washers and wipers, a fully functional heater, carpeting, my center console, an AM/FM stereo radio, and the side impact beams in the doors of the car, one of the reasons the doors on a second generation F-Body weighed so much.
But it was quite a bit lighter than stock 73 Firebird, and it was worth it.
Friday, April 14, 2017
The Story of an Old Firebird, Part 4.....
This section
contains information about the cylinder heads, valvetrain, and
intake/exhaust systems.
Heads and Valvetrain
-
For the cylinder
heads and camshaft, I planned on using the tried-and-true Ram Air IV
combination. The parts were readily available, reasonably priced, and
well understood by people I trusted.
I started with two
brand-new 1970 Ram Air IV castings, casting number 614. I remember
starting at the cast-in numbers “614” for HOURS as I ported the
heads. I don’t think I’ll ever forget them. The valves, springs,
retainers, locks, rocker arm studs, rocker arms, balls and nuts, push
rod guide plates, push rods, lifters, and cam were all 100% stock
Pontiac, purchased over the counter at Bert Adams Pontiac in Joliet,
Illinois. The timing chain and gears were a Cloyes “True Roller”,
and the cam was installed 4* advanced. When Jack installed the cam he
also checked the cam timing from the published specs, and found out
the cam was actually a few degrees retarded, as ground. Installing it
4* advanced made it basically “straight up” cam timing.
The first thing I
did with the heads was to clean up any casting flash and
“dingleberries” in the under-the-valve-cover and oil drainback
areas. There was a TON on casting flash on the sides of the intake
port runners, and some of it came off pretty easily. The rest took
some grinding, and made me glad I’d purchased carbide cutters. High
Speed Steel (“HSS”) cutters will remove cast iron easily, but
they go dull quickly, after only a few hours use. Carbide cutters
stay sharp, but they’re brittle compared to HSS, so be a bit
careful using them. I didn’t polish any of the areas with sandpaper
rolls as I couldn’t see the benefit vs the amount of time it would
take. The nice, sharp carbide cutters did a “good enough” job,
and after 10~12 hours, that part of both heads was cleaned up, and I
started to work on the ports. I also opened up the machined passages
in the heads for the pushrods. I’d read somewhere that it was
pretty close with the larger diameter pushrods the Ram Air IV used,
so I just “laid over” the upper end of the passage for a little
more clearance.
The book I used to
guide me in this engine rebuild was published by H-O Racing
Specialties, and was called “Pontiac Heavy Duty Parts and Specs”,
and had a wealth of information in it. I carefully studied the
cross-sectional drawings of the ports in the Ram Air IV heads to see
where material had to be removed, and just as importantly, where to
leave material. You don’t just go wild and “Hog It All Out”, as
the size and shape of the ports, particularly the intake ports, is
critical to how well they function. There were a couple of places
that needed careful work, like the port wall next to the passage the
pushrod went through, and the area under the valve seats. You had to
widen the intake port as much as possible in the pushrod area, but
you had to be very careful not to break through the casting. The
thickness of the casting in this area was about .125” thick
(one-eight of an inch), and while H-O said you could thin it down to
about .070”, I wasn’t comfortable enough with my head porting
skills to go that far, so I opened it up to where the wall was about
.080” thick. The book also pointed out areas that definitely needed
rework, like the valve guide are of the intake ports, the “bump”
in the exhaust port that was extra material for the air injection
(“Thermactor”) system, and a few other spots.
The basic philosophy
was again to “grind it out if it doesn’t look like it belongs
there”, and to keep as close as possible to the OEM contours,
opening them up where it would benefit airflow, and leaving material
in other places. The valve bowls needed a LOT of work. There were
huge “globs” of cast iron sticking out below where the cutters
that made the valve seat and bowl bottomed out, and this area needed
to be ground out to follow the “natural” contours in that area,
and blend it into the rest of the port. The head/intake manifold and
head/exhaust manifold flanges were matched to the gaskets I was going
to be using, and then blended back into the ports as smoothly as
possible, and as far as possible. Based on the 4 to 5 hours “per
session” that I spent, times 16 ports, plus the ~10 hours doing the
other parts of the head, I know that I had over 100 hours in the
heads by the time I finished them, and Jack complimented me on the
quality of the work I’d done. The final step was getting a proper
“Three Angle” valve grind done, and Jack did that for me. It took
some convincing to get him to grind the intake valve seats at the H-O
Racing recommended 30* instead of the “standard” 45*, but when I
showed him the published data in the H-O Racing book, he agreed, and
ground the intake seats to 30*. It cost a bit extra because he had to
buy a special cutter, but it paved the way for other Pontiac engines
he built for other people.
The combustion
chambers were almost “Good To Go” right out of the box, and all I
did was break any sharp edges that could lead to hot spots,
preignition, and detonation.
I didn’t weigh the
heads before and after, but from the pile of cast iron I ground out
of each port, I wouldn’t be surprised if I took almost a pound of
cast iron out of each head.
Camshaft, lifters,
and valve gear -
The rest of the
valve train was 100% 1970 Ram Air IV. The camshaft (P/N 9794041)
specs were: Advertised Duration 308* Intake / 320* Exhaust,
Duration @.050 232/242, lift at valve using 1.65 rocker arms -.520”.
Pontiac was at the forefront of “Computer Designed” cams way back
then, and the 041 cam, along with the 9785744 (Ram Air III cam) were
among the first computer designed cams released by GM. Prior to this,
many cams just added duration using the “constant dwell” method,
which resulted in what would be called “lazy ramps” today. I’m
not a camshaft designer, and I don’t play one on TV, but from all
I’ve read, you want the ramps to smoothly accelerate the valve
open, and do the same as it comes down the ramp. One of the reasons
racers went to roller cams was that the roller lifters allow much
more aggressive ramps, to get the valves open, and then closed, right
now. Roller
cams and lifters were a little too exotic (read: Pricey) for me back
then, so I stayed with a flat tappet cam, and what better cam to use
than the one designed by the guys that knew the cylinder head flow
characteristics? The Ram Air
IV lifters were of a special reduced travel design, and after the
engine was put together, I adjusted them ¼ turn of the rocker arm
nut past zero lash. I had considered using a rocker arm nut with a
separate locking screw, like a “Poly Lock”, but that would have
required having the ends of the rocker arm studs ground flat to
provide a proper place for the setscrew to tighten against, and I
just never got one of those “round tuits”. I readjusted the
rocker nuts one time after the engine had a few hundred miles on it,
and they hadn’t really changed any from the initial setting, so I
let it go at that.
It had a strong
“rumpity-rump” idle at about 1100RPM, but I most likely had to
run that idle speed due to the very light (12lb) aluminum flywheel.
Intake and Exhaust -
The induction
system would be a QudraJet, something I understood very well, with a
1971/72 455 H.O. intake manifold. This manifold had “as cast”
ports large enough to mate with the Ram Air IV heads, enough metal to
safely allow port-matching, was a modern dual-plane high-rise design,
and had a separate exhaust crossover which could be left off during
warm weather, resulting in a cooler intake charge going into the
engine. All I did to the intake manifold was to glue on a set of the
intake gaskets I’d be using, and open the ports up to match the
gasket. Then I blended that area back as far as I could reach with my
die grinder. The only other thing I did was to use an aluminum “heat
blocking” plate that had a fiber spacer about 1/4” thick on one
side, and a gasket on the other, that went between the carb and
manifold flange. I don’t know for sure if it helped any, but it
looked pretty neat! This was recommended by the “Rochester
Carburetors” book that I had. That book taught me more about
carburation than any other book I read, including the “Holley
Carburetors” book that I had by the same publisher.
The QuadraJet I used
was purchased new-in-the-box through Bert Adams Pontiac, and was for
a 1969/70 Ram Air IV with a manual transmission. It required one of
the spring type choke coils and pull rod, which I also ordered new.
Being a 1970 carb, it was calibrated a bit on the lean side for
emissions reasons, and I wound up going 2 or 3 sizes larger on the
main jest, along with a corresponding change in the primary and
secondary metering rods. I wish I still had my notebooks, as I had
extensive notes on how I figured out what a good jet and rod
combination would be based on what was in a given car from GM, vs
what it needed to be for better performance in various stages of
tune. I re-jetted dozens of QuadraJets based on these calculations,
and it was unusual that I didn’t get it “right” the first time.
Exhaust duties would
be handled by a set of Hooker Headers, part number 4202, the only
header available for the round port heads in a second generation
Firebird. JR Headers also made a set that fit, and one of my friends
had a pair on his 1973 Super Duty 455 Trans Am, but I thought the
Hookers were made better, so I went with them. Mufflers were kind of
an afterthought, and for years I was running Thrush “header
mufflers”. They were cheap, lightweight, and worked “good
enough”. Cheap was important, because the Hookers hung down fairly
low, and with the lowered suspension I was always grounding them out,
resulting in the muffler getting damaged enough to need replacement.
I used to buy them two at a time at Sontag Speed Supplies. That way I
always had one “in stock” for rapid replacement. I ran the
exhaust in that configuration until I drove the car out to
California, and which time I had a local muffler shop weld up some
2.5” pipes to the “Hemi” mufflers I’d bought years earlier.
It made the car much quieter on the highway, an important
consideration since it would be a 2,400 mile trip.
Fuel System -
The fuel system
starts at the tank, and in order to provide an “unlimited” supply
of fuel, I added a second 5/16” pick up and nylon “sock” filter
to the existing stock pick up/sending unit. I just used a piece of
5/16” steel fuel line, bent to match how the stock pick up was
made, drilled another hole into the top of the plate that mounted
into the tank, and silver soldered the new line to the top plate.
These two lines fed a pair of AC Delco electric pumps which were
originally used on heavy-duty trucks that I bought from North Side
Auto Parts on Ruby Street. If I had a part number, they could usually
get what I wanted! The pumps had individual fuses, and were fed by a
relay activated whenever the ignition was in the “Start” or “Run”
position. The output of each pump went through an AC Delco filter,
and then into a Moroso “Y Block” which was normally used to split
a single fuel line to be used with a dual-inlet Holley carb. From
there, a 1/2” diameter line was run to the engine compartment and
connected to one of the blue Holley pressure regulators set at 6.5
PSI. One outlet from the regulator fed the QuadraJet, and the other
was adapted down to 1/8” steel line which I ran to a fuel pressure
gauge in the console. I know, having pressurized gasoline fed to the
interior of a car is not a Real Good Idea, but I used steel
line with compression fittings and checked it religiously for any
signs of leakage. The fuel pressure NEVER budged from the 6.5 PSI I
had it set to, indicating that the carb had an adequate supply.
Tuesday, April 11, 2017
Chuck to the Rescue!
Found on the Book of Farce.
It was too good not to share......
More Pontiac stuff coming soon, tonight or tomorrow.
It was too good not to share......
More Pontiac stuff coming soon, tonight or tomorrow.
Monday, April 10, 2017
Grandbaby Update....
Little guy is over FOUR pounds now, growing like a weed, and can finally wear some of the clothing everybody has been sending to his parents.
He's out of his "isolette" and into a regular crib, and is using his pacifier when he's not wolfing down food.
Say "Hi!" to the nice people, Noah....
He's out of his "isolette" and into a regular crib, and is using his pacifier when he's not wolfing down food.
Say "Hi!" to the nice people, Noah....
Thursday, April 6, 2017
The Story of an Old Firebird, Part 3...
This section of
“Jim’s Old Firebird” will cover the engine I built for it, why
I made the choices I did, the parts I bought, and how it worked out.
This section covers the block and rotating assembly, commonly called
the short block.
Design Philosophy -
In deciding what I
wanted (It HAD to be a Pontiac engine!), I looked at what was
available for my intended purpose, which was high-performance street
usage, and road racing. Since I didn’t want maximum torque at
minimum RPM, I went with a 400 CID engine size. This gave me what I
considered the “best” bore-to-stroke ratio, allowing good torque
at midrange RPM (important for exiting corners), while winding high
enough to produce good horsepower for the straightaways.
Durability was to be
paramount in this engine build, so I had to look carefully at certain
items, namely the crankshaft and connecting rods. Good, reliable
pistons were easily available from companies like TRW at very
reasonable prices, along with high-quality piston rings, main and rod
bearings, oil pumps, timing chain and gears, and other things, and
the block was deemed suitable by several knowledgeable people. I’ll
cover the crank and rods decision, and why I used those pieces, in
the “Rotating Assembly” section.
My selection of
parts, and this design philosophy, was guided by the wisdom of the
guys at H-O Racing Specialties in Hawthorne, California. They had run
a series of NHRA record holding cars, and published a book that laid
out everything they’d learned about making Pontiacs run strong and
last. They also knew the difference between squirting down a
quarter-mile, and competing in a road race, and were great guys to
talk to on the phone. My selection of a machinist/engine builder was
based on reputation and recommendations from several local guys who
knew what they were talking about.
Block -
All good structures
start with a good foundation, and an engine is no exception. After
consulting with H-O Racing Specialties in Hawthorne, California, and
my engine builder Jack Waldvogel, I decided to keep the two-bolt main
block that came in the car. H-O confirmed that for my intended
application, the stock block was plenty “good enough”, and my
engine builder confirmed that he’d never seen a two-bolt main
Pontiac block fail except under the most extreme use, and then it was
almost always a rod letting go, and ventilating the block. This was
also a “seasoned” block, having gone 24,676 miles in a street
car, and numerous heat/cool cycles which help stabilize the cast-iron
in the block.
I spent many hours
with my Sears die grinder deburring the block of any and all casting
flash and “dingleberries” inside the block that could possibly
break off and contaminate the oiling system. There were several small
pockets of casting sand/cast iron mixture inside the block that I
knocked out, and a ton of casting flash. My strategy was if it didn’t
look like it belonged there, it probably didn’t, so I ground it
down. The lifter gallery in particular had a huge amount of casting
flash which I ground away. I also “radiused” all the oil
drainback holes and passages, and broke all the sharp edges inside
and outside of the block to eliminate any possible “stress risers”
where cracks could start. I didn’t go to the extreme of polishing
things inside like the NASCAR and Road Race guys do, as I didn’t
see the benefit of it. It was pretty shiny by the time I was done,
though. I also didn’t paint the inside of the block with either
General Electric “Glyptal”, an oil-resistant electric motor
paint, or Rustoleum, as I’d heard too many horror stories of the
paint coming loose and causing extensive damage to the engine. Unless
the surface is EXTREMELY clean, the chances of the paint peeling off
were just too high for me to accept.
As soon as I’d
collected enough parts for Jack to get started, I took them all down
to his shop so he could get started.
Jack was a great
guy, and it’s sad that he’s no longer with us. He was a
first-class machinist, welder, and assembly guru, as well as being an
all-around Good Guy. My Dad knew his Dad from the Navy, and my Dad
sold Jack his Bridgeport milling machine, a variable speed “2J”
head, and a ton of tooling; a first-class Bridgeport setup. Jack had
also served in the US. Navy, and served time as a Machinist Mate on a
nuclear submarine.
Jack bored the block
.060” oversize, honed the cylinders on his Sunnen machine, and also
decked the block to “square it up”, and align-bored the main
bearing bores. He drilled and tapped one of the small press-in plug
holes in the block so he could install an Allen setscrew in there
that had a small hole drilled in it to squirt oil on the
distributor/cam gears. This was a modification suggested by H-O
Racing to keep the gears properly oiled. “High Tech” stuff at the
time, and in common use these days. All other “small” pressed-in
plugs were replaced with Allen setscrews, and the “freeze plugs”
were replaced with brass ones. The completed short block was painted
black after final assembly. I requested Jack leave the oil pan off
the engine, as I wanted to get some pictures of the bottom end, with
those pretty Carillo rods. Sadly, I lost those pictures many years
ago.
Rotating Assembly -
Since the connecting
rods are generally considered to be the most highly-stressed parts in
the engine, getting “good” rods is a must. The rods alternately
get stretched/pulled apart when the piston is being yanked down the
bore during the intake and power stokes, and then squeezed together
as the piston goes back up the bore during the compression and
exhaust strokes. So, you need to make the rods out of a material that
can withstand both tension loading (“stretching”) and compression
loading (“squeezing”) without failing. Forged steel is the ideal
material for this application, and it’s what almost all “good”
connecting rods are made from.
Unfortunately,
Pontiac didn’t make most of their rods from forged steel, opting
instead to save some money and make them from CAST steel, which they
called “ArmaSteel”. For most purposes, like the 400 2-bbl in
Mom’s Catalina station wagon, it’s plenty “good enough”. For
a 400 CID engine spinning 6,500RPM it’s borderline, and for a 455
turning anything more than 5,700RPM, it’s a disaster. The bad thing
about cast materials is that when they fail, they FAIL, almost always
by coming apart, a Real Bad Thing to happen to a connecting rod.
So, what choices did
I have? Well, I could try and hunt down some 389 Super Duty rods
(somewhat available), I could try and beg, borrow, and spend my way
into a set of 455 Super Duty rods (chances were slim to none, and
Slim just left town), I could get some aluminum rods (NOT! Aluminum
lacks the cyclic fatigue strength needed), or I could bite the bullet
and order some Carillo Rods. These rods were absolutely the best you
could buy at the time, and had an unbeatable reputation. I was told
by my engine builder that he’d sent one back that was bent due to
an engine failure, and Carillo straightened it, Magnafluxed it,
installed new bolts, completely checked it out, pronounced it fit for
service again, and sent it back to him “NO CHARGE”. That’s
about as good as it gets!
So, taking some
advice from H-O Racing, I went ahead and ordered a set of rods
through Sontag Speed Supplies but had them made .230” LONGER than
stock. The advice from H-O was, as long as you’re paying to have
these rods custom-made for you, why not take advantage of the fact
that they’ll make them any way you want, and get them made longer?
This way, you get the benefits of a basically indestructible
connecting rod, AND you get the benefit of a “better” rod
length-to-stroke ratio. The rod length-to-stroke ratio is one of
those things that you never hear talked about much, especially “Back
In The Day”. The benefits are lower peak piston speed and
acceleration (reduces stress on the piston, pin, and rod), longer
piston “dwell time” at TDC and BDC, and lower piston side
loading, which is how hard the piston pushes against the cylinder
wall.
Why the importance
of longer dwell time? Well, for one, it lets the cylinder both fill
better, and evacuate better, making the engine more efficient, and
maximizing the cam timing it has.
Since I’d be using
longer rods, I’d have to buy special, custom made pistons, right?
Wrong! I chose the length to be .230” longer than stock, which is
exactly the difference in where the piston pin hole is located
between a 400 piston and a 455 piston. I was able to get a set of “30
over” 455 Super Duty forged pistons ordered through Bert Adams
Pontiac. These pistons were made by TRW, and had the advantage of
having a single “eyebrow” valve relief in them, rather than an
“upper” and a “lower” valve relief. This raised the
compression ratio slightly, and was proven to flow better than having
two valve reliefs in the piston. Remember the longer “Dwell Time”
I mentioned? Since the piston is now spending more time at TDC, the
piston crown essentially becomes a part of the combustion
chamber/intake port “system”, and things you do here can have a
big impact on the “Total Flow” in and out of the engine. All I
did to them was break the sharp edges with a Dremel tool. The rods
needed exactly ZERO work
done to them. Jack told me they were balanced as good as he could do
it right out of the box. The day they came in at Sontag’s, Bill
Sontag asked me if could open the box so he could check one out. He
looked at it, smiled, and said “Yep, it’s a Carillo rod”. About
the same time Ron Menzer came running out of the back like a kid on
Christmas morning, and asked if he could hold one. He oohed and ahhed
for a few minutes and then handed it back and said “THANKS”.
So, with rods and
pistons covered, I moved on to the crank, flywheel, clutch, and
harmonic balancer.
There were few
Pontiac cranks made from forged steel that had the required 3.00”
diameter main bearing journals. The 389 Super Duty had one, as well
as the mythical Ram Air V engines, but that was it. Moldex was about
the only company at the time that would make you whatever you wanted,
but that wasn’t in the budget for me. I looked around and contacted
a few people, but nobody had any 389 SD cranks for sale. SO….turning
to H-O Racing again for guidance, I decided a 1970 Ram Air IV cast
nodular iron crank would be my choice. It was made of a better grade
of cast iron than my 1973 crank, had better heat treating, “rolled”
journals, generous “fillets” on the journals, and some other nice
things I forget now. Best of all, it “only” cost about $135! Jack
“micropolished” the journals after he radiused the oil holes, and
did some deburring of it, but that was it for the crank.
I wanted to use an
aluminum flywheel because a lighter flywheel has less rotational
inertia, meaning you can accelerate it faster which translates into
faster acceleration once you’re moving.
This means you can accelerate harder out of corners, a perfect fit
for a car I planned to road race. Why do drag racers use heavy
flywheels? Because a heavy flywheel can store a lot of energy which
gets released when the clutch gets popped, making the car accelerate
harder from a standstill
IF you have the traction (Slicks) to use it. Otherwise you’ll just
blow the tires away. The first flywheel I bought didn’t fit the
crank, so I talked to Tony at the parts counter, and he confirmed
that the early and late flywheels all the had the same number of
teeth on the ring gear, so I told Jack to go ahead and machine the
flywheel to fit the crank. BIG mistake! It turns out the older
flywheels were “flatter” than newer ones, and the first time I
tried to crank the engine in the car I was greeted with the stater
going “ZIIIING!”, and not engaging the flywheel. I checked the
part number I ordered with Sontag, and sure enough, it was for a very
early Pontiac V8.
I should have suspected something as the box it came in looked older
than me, and had an inch of dust on it. Oh, well, order another
flywheel, and this time make sure it fits a 1970 Pontiac!
In
order to keep rotating mass small (because….Road
Race!), I stayed with a
10.5” pressure plate and clutch disc. The pressure plate was a
Borg-Warner “Power Brute” unit, and the disc was for an L88
Corvette. I used a
Borg-Warner “Power Brute” clutch release (throw out) bearing as
it had a different bearing design than an OEM release bearing, which
was supposedly longer lasting when used at high RPM. I never had any
trouble with the clutch, and it engaged solidly, never slipping. The
pilot bearing in the end of the crank was a standard GM pilot
bearing.
The
harmonic balancer was for a 1970 Ram Air IV engine, and I had Jack
“degree” it, cutting timing marks and stamping numbers on it so I
could easily set the initial timing, and check the total timing.
Other
Engine Related Parts
-
I
used an OEM Ram Air IV oil pump along with an H-O Racing higher
pressure relief spring. I took the pump apart and brazed the pickup
tube and screen into the body so it couldn’t fall out, and also
checked the clearance between the gears, the gears and the body, and
the gears and the end plate. I carefully sanded the open end of the
pump body using some 600 grit wet-or-dry sandpaper on a glass plate,
with plenty of oil, and did the same to the end plate to make sure
they were FLAT, and had a polished finish. This ensured there was no
gap between them, reducing any chance of losing oil pressure.
Since
this engine didn’t come with one, I ordered one of the “3/4
length” windage trays listed in the Pontiac
parts catalog. I
used the stock oil pan as it had a baffle in it to keep the oil in
the pan near the pickup, but it only worked well in left turns! The
car cornered so hard that I constantly had to watch the oil pressure
in right hand turns, as I could make the pressure drop just
“twitching” the steering wheel hard to the right! Even running a
quart over didn’t help too much, and this was an issue that plagued
me the entire time I owned the car.
The
water pump, was a Moroso aluminum unit that saved a little over two
pounds. As I mention later, weight saving was another big item to me,
and eventually the car wound up about 400 pounds
lighter than when it rolled out of Norwood. The
front cover was the one that came with the car. I had Jack check the
timing badge to make sure it agreed with the degreed harmonic
balancer, and it did.
In
the end, the only parts that I used that came with the car were the
block, the valve covers, the valley cover, the front cover, the oil
pan, and the oil filter adapter. I had a set of chrome valve covers
from a GTO, but they didn’t have the oil “dripper” rails
inside. Since I read that this could cause your rocker arms to fail
from lack of lubrication, I painted the stock valve covers wrinkle
finish black, and put them back on the car. I also kept the Unitized Ignition distributor. I carefully shimmed all the end-play out of the gear at the bottom, and replaced the stock gear with a bronze driven gear I bought from H-O racing. This turned out to be a mistake, as about 1,000 miles after I got the car running, the teeth wore through, and the engine quit running when I was at the Car Craft Street Machine Nationals in Indianapolis. I was lucky that it was my last night at the hotel. My friend Marvin gave me a ride home, and then took me back the next day to fix the car, and get it back to Joliet.
"Car People" are good people, always willing to help a buddy in trouble!
"Car People" are good people, always willing to help a buddy in trouble!
Subscribe to:
Posts (Atom)
The Legacy of the American Racing Equipment "Torq-Thrust" Wheel
Americans were always my favorite "mag" wheel. I had them on my little Ford Capri, both of my Corvettes, my El Camino, my race ...

-
Yawn....just more Kabuki Theater, but interesting reading, nonetheless. Read All About It Here.....
-
Every so often when I'm checking my PiAware ADSB receiver/display I'll notice an aircraft with a flight path that catches my eye. I...